Job Scope :
To perform Acis stimulation due to decline in production
Well History :
Drilled March 2001- FTHP:3800psi FLP:2000PSI
March 2012; FTHP: 932psi FLP:612psi
Fishing Operation: Observed carbonates in wire
May 2013: FTHP 1725psi FLP: 55psi
August 2014 : FTHP: 232psi FLP: 102psi
April 2019 : FTHP :93psi FLP=58psi
Design Consideration
Jetting Nozzle
Coil Tubing to reach TD – Circa Simulation
Injector to provide the required pulling capacity as per simulations- TFA Analysis
Acid Strength – 15%HCL Acid System
Chart Explanation
- RIH CT & Performed weight checks for every 305m gained.
- CT TAG HUD @ 3309m. (Suspected to be an XO from 41/2” Tubing to 31/2” )
- Pumped 10bbl of 10% HCL acid to Pickle Production Tubing and displaced acid with 184bbl of 2% KCL brine
- Closet CT/Tubing annulus & performed injectivity Test.
- Acid Treatment with 15% HCL Acid Recipe @ 0.8bpm
- Commenced Nitrogen Lift Operation @ 2000m
- CT park @ 1800 jetting nitrogen with returns of brine and spent acid received on surface
- CT on surface; WHP=1365psi. With crude oil returns on surface.
Conclusion
- Job was performed successfully with no incident and as per program
- Lined up well to flow station with FTHP=1150psi and FLP= 159psi on a choke of 16/64